THE BUILD

Engine

Ruth's comments

 

 

As mentioned on the “Preperation” page, the Yamaha R1 engine was selected for its good bang for your buck. I managed to get hold of a 2003 spec injection engine. The injection system gives a little more power than its carb old brother, and a broader power band.

It is an impressive package, its just so small and light:

I can pick it up on my own

 

This was left with Zcars and came back all set up in the frame, as you can see from the photo:

Engine in frame, with all rear drivetrain, waiting to be fitted

We had fun and games fitting the frame into the body shell. You don’t want to cut too much metal off but its a tight fit. It was a case of lifting the body over the frame...does it fit? No! cut a bit off here and there and try again. Once in, its a simple job of bolting the front part of the roll cage to it, making sure its all square and bolting it to the shell.

Cooling

Was took a little thinking about, the Yamaha radiator has a lot of connections, mine has the basi in and out. The diagram below shows how I plumbed it

Engine plumbing diagram

Which ever way its done it uses a lot of hose and the system has a pretty large water capacity. Don’t under estimate what a difference boxing the engine in behind the bulkhead makes. Without the bulkhead and rear wndows the system would regulate it self at 80oC just on switch of the thermostat. Once it was all boxed in behind the bulkhead it needed the fan t oswitch in and out. This was a little un-nerving as that doesn’t happen until 99 oC! A little hotter than I’m used to seeing on cars. Once the fan switches it, it quickly drops to 92 oC.

Fueling

Check out the seperate fueling section.

 

Throttle

The throttle linkage was a tricky one to get right. Obviously the linage is long, Zcars supply an 8foot long cable. But getting this cable to have a smooth action is tricky. The original instructions are to drill the throttle linkage to move the pull point on the shaft lower, reducing the amount of cable pull. Then run the cable into the front engine bay, down the transmission tunnel and up to the throttle bodies. This requires a 180degree tight turn in the cable at the pedal end, resulting in a lot of drag. Now Zcars have a lever that bolts on to the front sub frame. A short cable goes from the pedal to this lever and the other end to the 8 foot cable, so this turns the motion through 180degrees. This works well, once some extra return springs have been added to the new lever.

Another throttle linkage problem is at the throttle body end. The end to the cable can flop about on top of the cable stop. Adding a support to this and using the lock nuts to bolt the cable to the stop makes for a better throttle action. With too much slop there, the throttle sometimes wouldn’t shut fully..

 

 

Clutch

The clutch setup of the zcars/R1is to use the original mini master cylinder up front, original slave cylinder at the transmission end then modify the cable pull clutch actuator to a push rod by welding some M6 stud to it. My first problem was that the zcars positioning of the chassis tab to bolt the slave cylinder is at the wrong angle. It points the cylinder to the wrong side of the pivot point meaning that at full extension the push rod is at a silly angle. I solved this problem by shimming the slave cylinder out to the correct angle.  The next job was to make an adjuster. I bought some 8mm steel rod that just nicely slipped over the M6 stud and with a nut on the stud as an adjuster it was sorted.

Next I ran into trouble! I had made the adjuster too short, I stood on the clutch and popped the end out of the slave cylinder. I stripped it down and decided it wasn’t worth repairing. The bore was scored and the seal damaged, as replacements were only £20 for the complete cylinder I just ordered a new one.

With a new slave fitted and a correctly sized adjuster I tried the clutch. It wasn’t clearing...bugger. It had worked before. I had read on some web page or other R1 clutches can stick if they had been over pushed...it was time to take the cover off and look at the problem. I found bike clutches are very easy to strip and rebuild, the problem, I think, was lack of use. A bike clutch is a wet clutch, but with the engine being stood for so long the clutch was dry and had stuck shut. I gently released the plates, bolted it back together and hey presto, the clutch worked. I adjusted the clutch so that bottoming out the pedal didn’t take the actuator beyond its limit or the slave cylinder beyond its max.

 

 

Exhaust

The system came with the kit, so didn’t need a lot of work. The ting that needed thinking about was heat management. The headers come down the front, close to the bulkhead so the headers need lagging in exhaust wrap. A bargain from E-bay got me 100 foot of wrap for £20, compared to Deem Tweeks at £1 per foot, as was very happy!  I lagged the system right down to where it disappears in he 4 to1 collector under the sump. I also lagged the accelerator cable with it along with some reflective heat shield. The handbrake cable and electrical cabling anywhere close to the exhaust also came in for some lagging.

 

I fitted the silencer when the car was on axle stands. On fitting I thought it might be a bit short on ground clearance. On dropping the car on its wheels I found the clearance to be all off 5mm (memories of the Tiger’s grounding sump came flooding back to me). I’d noticed the Zcars demonstrator had a cut out in the rear valance to allow the exhaust to be raised, so I chopped a semi-circle in mine to get a couple of inches clearance. There’s stacks of room, so an oval exhaust can would buy another inch, or an exhaust across the rear valance would be better...all options for the future.

 

 

  

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