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Differential Work
Parts used:
Again, with my attempt to do as much of this work as I could myself, I decided to tackle the differentials. Many thanks go out to Jeremy Little and the others at Randy's Ring and Pinion for providing so much help. They never suggested that I just send the diffs to them and let them do it. Even when I called to order tools, Jeremy told me what to do to avoid the expense. I chose the rear 9-inch differential to start with. Since I had already had the diff rebuilt and a Detroit installed, I knew that it would be a lot less work to complete. After removing the diff from the rear housing, I completely disassembled the case. I pressed on the new pinion bearings with a new seal and set the pinion preload. This was pretty tough to do. I eventually ended up with two 6-foot breaker bars to collapse the sleeve and get the preload right. Once the pinion was in, I installed the Detroit with the new ring gear installed and tried to set the backlash. As the backlash got close to being right, the sharp click of the gears hitting each other turned into a thud. It turns out that the 4.56 ring gear hits the pilot bearing support in the case. I stripped the entire case apart again and ground the support slightly to clear the gear. After a thorough cleaning, I reinstalled the gears and proceeded with the setup. Pinion depth only required three tear downs to get right. Once the backlash was set, I cranked the adjusters tight and gave everything a final torquing. The final step was to recheck backlash and check the gear pattern around the entire ring gear. It all looked good, so back in the truck it went. So far, the front Dana 44 has me pretty worried. It requires that the bearings be removed to change all of the adjusting shims. I get nervous pulling bearings over and over, it's an invitaion to disaster. I'll finish that write-up when I get it done. Turns out the D44 was very time consuming, but not as difficult as I had feared. Here's a few pics to hold you over until I can get the story finished.
The tricky part of pulling these bearings was not tearing up the shims under the bushings. With a little practice it got pretty easy. I used my hydraulic press to reinstall the bearings. In total, I had to remove and replace the bearings about eight times. The old bearings were used for all checks. The new bearings were installed after all clearances and preloads were checked. A final check of all measurements verified that nothing changed with the new bearings.
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