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As I mentioned before, the car experienced significant detonation at around 4300 RPM's.  In addition to the fuel problem I believe there was insufficient air flow through the intercooler.  
Here you can see the car being run on the chassis dyno.   You can also partially see the custom 3" exhaust.  dynoshot1.jpg (43117 bytes)
Here is another picture of the car being prepared far a run.   You can see the Spearco Intercooler under the car. dynoshot2.jpg (37459 bytes)