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WHISKY INFERNO - $300,000 LOST IN HARBOUR BLAZETranscript of newspaper article - Sydney Morning Herald? 24.11.68
Fumes from the burning whisky overcame a 20 years old deckhand, Thomas Williamson, of Scotland. Late last night he was under sedation in Balmain Hospital. The whisky was part of a special Christmas consignment aboard the Suevic berthed at Glebe. It was in 200 casks, each containing 44 gallons of undiluted and extremely inflammable Scotch. Importers would have added equal to 40 per cent of it’s volume to bring it down to the strength people buy in hotels. This diluted scotch, which costs $4.54 for a 26oz bottle, does not burn. But the undiluted scotch and the wooden casks flamed fiercely in the Suevic’s hold, giving off thick black smoke. Firemen at first tried to smother the blaze with foam. Then they pumped 1,600 tons of water onto it. Today the Suevic is leaning over at a drunken angle because of the combined scotch and water. Beside the Suevic, firemen set up a mobile kitchen. It served soft drinks and hot dogs – no scotch. The skipper of the Suevic, Captain J.P. Mason, said “It was terrible to see all that scotch burn. The men’s eyes were streaming at the sight of it.” Sipping an Australian beer, Captain Mason said: ”The ship was awash with water and whisky.” He said it was a pity about the scotch, but the firemen and crew had done a magnificent job in their six hours bout with the whisky.
SEAMAN SOUGHTNew Plymouth, Friday May 1st 1970
New Plymouth Search and Rescue authorities feared last night that the Scottish seaman who has been missing from the Shaw Savill cargo vessel, Suevic, since Wednesday has drowned somewhere in Port Taranaki. Clothing identified as belonging to the missing man was found under the Newton King Wharf at about 2.39pm yesterday. The controller of New Plymouth search and rescue, Sergeant V.R. Story, said last night investigations suggested that the missing seaman, Mr Murdo John MacKenzie (24) had taken his own life by drowning. Scottish born Mr. MacKenzie, an able – seaman on the Suevic, was last seen at 7.00pm on Wednesday sitting in a dazed condition on the Newton King wharf. He was not reported missing to the police until 11.50pm. Extensive local inquiries by police and the ship’s crew had revealed nothing by yesterday morning. The search continued yesterday morning, backed up by radio broadcasts, and Mr. Story said it was intensified at about 1.30pm when a more detailed search of of the harbour area was begun. At about 2.30pm a policeman sailing underneath the Newton King wharf in a small boat returned with several items of clothing identified as belonging to Mr. MacKenzie. ClothingMr. Story said the clothing, a pair of jeans with a watch and some small change in their pockets, shoes, socks and underclothing, had been found lying over a fuel pipe-line that ran underneath the wharf. “The small recess that leads to the hatchway to the pipe-line was only about 20 yards from the Suevic’s gangway,” he said. The pipe-line was only about 5ft from the water and, because Mr. MacKenzie was believed to have been in a disturbed state when last seen, Mr. Story said it was assumed that the missing man had jumped into the harbour from the pipe. At about 4.15pm two members of the New Plymouth Underwater Club were called in to make a search of the area near where the clothing was found. The search continued until 5.00pm, when it was called off until tomorrow morning because the water was too dark for a thorough search to be made. Mr. Story said the underwater search would be resumed at 9.00am, today, and four under-water club divers used. Amateur divers were being used in the search because all the Taranaki Harbours Board divers were out of the area on another job. If, as believed, Mr. Mackenzie had drowned somewhere in the Port, today’s underwater search would be extensive enough to find the body. The Suevic is scheduled to sail from Port Taranaki next Wednesday for Auckland and then overseas. One of the last men to see Mr. MacKenzie was able-seaman P. Payne. A close friend of the missing man, Mr. Payne said: “He has been sick for more than a week and he really should have been put ashore at Lyttleton because there was definitely something wrong with him.” Mr. Payne, who was in the ship’s mess hall when the clothing belonging to Mr. MacKenzie was identified by crew members, said “ I was worried about him on Wednesday night when he was sitting on the wharf and after a while I went looking for him. I was still shouting along the dock at 10 O’clock.” Other crew members confirmed Mr. Payne’s observations about Mr. MacKenzie’s condition when last seen and one suggested that there should be an investigation to find why MacKenzie had been allowed to remain on the ship in such a disturbed condition. Body Found A body recovered from the sea at New Plymouth Port yesterday is believed to be that of a seaman missing from a Shaw Savill cargo ship, the Suevic. On April 29 Mr. Murdo John MacKenzie, a Scotsman, went missing and his clothes were later found beneath Newton King wharf. About 7.00am yesterday, a member of the Suevic’s crew saw the body floating near the stern of the ship. Police recovered the body, which has not yet been positively identified.
On Saturday afternoon, wharf police received a call from the captain of a ship berthed at Wellington, who said that his vessel was “infested” with uninvited women, the magistrate’s Court was told today. Twelve women pleaded guilty before Mr. R.D.Jamieson SM to being aboard the Suevic without lawful excuse, and were fined $10 and costs each. They were: Diane Rowana White, 17 unemployed kitchen maid; Denise Reith O’Neill, 21, photographer; Margaret Royal, 29 unemployed; Robina Shaw Saunders, 20 toll operator; Pai Cowan, 18 receptionist; Jacqueline Harris, 24 domestic; Lynette Michele Jacobson 18, factory hand; Sally Anderson, 20 unemployed; Lydia Pauline Capper, 19, unemployed; Linda Mary Cowan, 20, receptionist; Anne Solomon. 21, cashier; and Lorraine Fay, 20, unemployed kitchen hand. Detective Sergeant D.E. McEwen said that at 12.30pm on December 13 the wharf police were called to a ship berthed at King’s Wharf, after the master had informed them that his vessel was “infested” with uninvited females. A passbook check on the ship showed that no passes to visitors had been issued, and that no visitors had in fact been escorted on board. The ship was searched and the women were found in the crew bar and in the crew accommodation. Several said they had just walked on board, and a number had stayed all night. Visitors with passes were allowed on board only between 6pm and 12pm, said the prosecutor. At the time the women were on board, he said, the ship was supposed to be working. The mass presence of the women had meant that the men were not working. This also inconvenienced the wharf workers, as the ship was scheduled to be loading at this time. Mr. M.A.Bungay, who appeared for White, said that there was no suggestion of immorality. His client had not stayed all night. Mr. M.C. Mitchell appeared for O’Neill, Royal, Saunders, the two Cowans, Harris, Jacobson, Anderson and capper. He said they had in fact been invited on board, but not by anyone with the authority to do so. None of those he represented had stayed all night. Mr. Jamieson said the object of the exercise had probably been largely achieved when the master relieved his ship of the “infestation.”
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