Modified 1984 Ford LTD

 

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1998 - The beginning 
     The Ford LTD I am using for my  "Sleeper" project is a midsize 1984.  I found this car for sale by a mechanic for "about $500" but it was after hours and nobody was at the shop, so I sent my wife to look at it.  About an hour later I got a phone call from her saying she bought the car for $200!  She brought $160 hoping to get him to go as low as that, but to no avail.  When she got it home I took a good look at it and was surprised to see it was in decent condition for the money. 
     The car was a base model with roll up windows, but it did have power locks, cruise control and air conditioning and over 175,000 miles on its 3.8 V6 drive train.  It ran great.  The transmission slipped a bit on the highway but for $200 who could complain.  We drove this car everywhere for almost a year and a half with no problems at all.  The only money we spent on it was for gas, oil changes and windshield wiper blades.  We were really lucky to find a car this good for such a low price. 
     After driving the car for a year, a good friend of mine gave me a great deal.  Vinnie's plans for converting a 1988 four cylinder Mustang over to a 5.0 H.O. motor fell through at the last minute.  Little did he know at the time that his Mustang would become a magazine project car and be converted anyway!  He knew I wanted to do a V8 swap so he sold me an entire 1988 Mustang LX 5.0. automatic for $400.  What was supposed to be his donor car, was soon in my driveway.  This Mustang was twisted like a pretzel after a high speed collision but all of the mechanical parts were good.  In order to remove the driveline I had to spend a day cutting the nose off of the crumpled Mustang.  After I removed everything of value for the motor swap project, including the 8.8 rear end, wiring harnesses, and all of the little bits and pieces that would make my life difficult had I not grabbed them, a local junkyard took the remnants away the next week. 
     So after all the work to get the parts out of the Mustang, I let it sit for six months waiting for the ambition to start such a big project.  Then one day my LTD just shut off after going over a speed bump in a parking lot.  Although it was probably just the ignition module I said "why bother fixing it when I have a 5.0 sitting in the garage".  That was the last my wife saw of me for two months! (See the Tech Page for more info on the actual conversion.)
      After I was finished I took it to Englishtown, NJ to try it on the drag strip, only to run a disappointing 15.4 seconds at 92 miles per hour.    My friends thought 15.4 was a good number for a heavy "family" car with an automatic.   When I got over being mad, I adjusted every sensor that had an adjustment and even a few that  "can't be adjusted".  Then I tuned everything that could be tuned, and at my next outing I ran 14.7 seconds at 95 miles per hour.  Now I was in the right time zone. 
     Since then I have added Auto Specialties Under drive Pulleys, a Moroso Cold Air Kit for a Mustang (I had to cut a little of the inner fender), and skinny front tires.  I still have the original 7.5 inch rear with 3.27 geared open differential (no traction loc).  Getting traction is a problem, but if I launch just right I can run 14.62 seconds at 97.89 miles per hour with a 60 foot time of 2.223 seconds.  I average 14.50s at 97 mph with a 60 foot time of 2.335 with street tires in back.  My best run to date (March 29, 1999) is a very repeatable 14.337 at 96.888 miles per hour with a 60 foot time of 2.164 seconds.  This was with Hoosier Quick Time's Mounted out back. I lost one mile per hour due to increased rolling resistance of the sticky tires at the end of the track but it was worth it to gain a repeatable time.

May 1999
     Well, here it is May 1999 and I am in the middle of installing my new 8.8 inch rear with 4.10 gears and a Traction Loc differential.  I am hoping to run between 14.1 and 13.99 with the new gears.  I am also installing a drive shaft safety loop to keep the car NHRA legal.  Okay the rear is in and I learned something...  If you try to use Eibach's Mustang rear springs in your LTD it won't work!  When I lowered the car off the jack it was an inch off the bump stops.  That is a bit to low even for me.  50 pounds more on the rear bumper caused it to bottom out completely.   

Summer 2000
Okay I need more stall in the transmission and more power!  The 4:10s did nothing on the track.  I ran the same numbers as before! the short times are faster and my 1/8th mile time is a little better but the car can't use the traction the limited slip rear and Hoosier tires provide. Don't forget they put sticky traction compound on the track surface.   In fact it seems to lug off the line and run out of steam at the top of the track.  3.73s would have been a better choice for such a stock motor.  On the street the car feels like a champion, it pulls harder than ever and is even more fun to drive.  It will light the tires from a 20 mile an hour roll.  I know the car is faster just ask the guy in the 98 Cobra with the confused look on his face and many others.

Nov 2000
Well I broke down and sold the LTD to a good friend who makes me nervous when he talks about what he wants to do with the car.  Since he bought it he has put cats and tailpipes on it!  now he wants to set the timing to a stock 10deg.  Oh well Its not mine anymore so I need to let go...  That said we went to E-Town Raceway Park in NJ  for a Lincoln shoot out for MM&FF magazine (his brother is one of the editors).  They took pictures and recorded the time slips but I am unsure if the car made the story since its not a Lincoln (it did not).  He did manage a  14.2 second run (timing set to 14deg).  So I guess his changes so far were not to bad for the car.  Note: he is 100 pounds lighter  than me and it was freezing cold.  The gears seem to offset the cats and tailpipes. He has attended to some things that needed repair to make the car a better daily driver.  I used it as a mostly as a drag car  so I let some things go a bit. Anyway the near future looks faster as spring approaches.  Both him and his brother are quite creative and resourceful so lets hope for some low budget 13 second runs this season.

June 2001
OK, big surprise.  My 4.10 rear turned out to a 3.73 geared rear!  That would explain the lack of change at the drag strip.  I found out when my friend was investigating a drive line vibration after a day of thrashing at the track.  After that trip the car did not see the track again until it was sold to Keith (see below) but numerous improvements were made.  Wayne rebuilt the front end with some parts that I gave him along with some that he had or bought.  KYB Front struts, Ford Motorsports front control arms, 87 Mustang GT front sway bar, smaller more tasteful Autoguage
gauges, fixed the rear brake lines and more.  He drove the car around like this for a few more month before selling it to our friend Keith.  

From here down still needs to be finished

Keith added nitrous           fixed fuel pressure loss with a 255 LPH pump    had the gas tank resealed  2nd Lincoln shoot out >>  made it into mm&ff  Keith lost interest after the stock AOD blew up.  My friend Vinnie From MM&FF traded his 2WD Suburban tow vehicle (also with a blown tranny) to Keith  for the LTD.  Unfortunately Vinnie did not have the time to work on the car. So he sold it back to me.  He put in the highly modified AOD and a 10 inch converter that was in his Lincoln LSC.  He put the LSC back to stock so his father could use it.  LSC AOD's are a little longer than the AOD a Mustang uses so he sent the drive shaft out to be shortened and balanced.  This is where the trouble starts.

July 4th weekend 2002 
bought it back ex wife's disaster trip 
TRIP NOTES

August 2002
car now in my possession filthy full of spare parts and Mustang GT disk brake conversion

 

 

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